We came over to Rockland on June 9th and hooked up the batteries and loaded food on board. I hooked up the new solar panel as well as the old one. We set about scrapping the toe rail. We painted the bottom and launched the dinghy. I ran the mast wires under the cabin sole and into the hanging locker.
6/13- put approx 35 gallons of diesel into the new tank. I serviced all three thru hulls and attached wooden plugs to each. I had to clear a large blockage in the cockpit drain. It was mostly hair??
6/14- I replaced the filter in the Raycor filter. We then painter the toe rail and bow sprit with a coat of Cetol regular.
6/15- Launched today, everything went fine. On mooring #11 this year.
Alayne and Saryn left for California for a week and I had to drive them down to Boston. While they were gone I finished hooking the mast wires up to terminals in the hanging locker. I made water proof connections for the radar and VHF wires under the sole using rj-45 connections. I got the radar working although at first I could not adjust anything. Eventually I figured out how to adjust the things I need to adjust. However when trying to contact Kevin from Mid Coast Marine he kept blowing me off. I finally contacted Simrad and they said the new Halo 20 radar was not compatible with my NSS 8 chart plotter. That sort of pissed me off. It all seems to be working fine now except for some high tech adjustments I don't need. The wind instrument is still not working very well.
7/8- adjusted the valves on the motor today. Seems to start hard and needs an extra shot of fuel. It was suggested by some that it may be a dirty injector. I'll have to keep an eye on this
8/15- Moved the starboard forward cleat out 2" in order for it to clear the windlass better. I hope to move the hawse hole so that the chain goes directly down into the anchor locker. I also painted the trim around the 2 main hatches with some Brightside white.
9/6- I installed new towel racks in the head made out of teak boards. I removed the wind instrument and installed a compass in the hole. I still need to make a back for it. I painted the toe rail with another coat of Cetol Natural.
9/9- We were hauled today with 515.6 hrs on the motor meaning we put 49 hours on this season. There was 812 nmiles on the chart plotter giving us 438.3 nm sailed this year.
9/10- I added some fuel with 1 1/2 oz of Biobor JF and I added 30 oz of Stan-a-dyne on a recommendation from Joe. I also installed a garboard plug and painted marks on the anchor chain.